Following
an unbelievably busy few months, so busy in fact that I didn’t even
have time to update the blog, things have settled into a nice even
rush! All of the engine rebuilds have been successfully completed,
another head repair/gasket replacement on a Stag with chains,
sprockets and all that jazz has also been and gone and we seem to
have had a few fuel system issues with various customers vehicles.
There
have been a few injection problems on TRs one of which turned out to
be a very badly routed and undersized supply pipe from the tank to
the pump with another couple having injector issues. We have also
seen 2 TR6s both with replacement ignition switches fitted which have
been overheating and causing breakdowns in heavy traffic – one on
the M25! This looked at first like an overheating fuel pump causing a
misfire then cutting out completely, only to restart having been left
to cool down for a while.
What
it transpired was actually happening though was that partly due to
the ignition controlled feed from the switch to the fusebox being too
small (smaller than the original) and partly due to the fitment of a
Bosch pump in place of the Lucas unit (the Bosch unit draws more
current) and a couple of additional ‘modern’ add on pieces of
electrical equipment, the poor old switch was overheating and going
high resistant just to make things worse, until it failed to pass
sufficient current for the ignition coil to function.
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